New safety conditions set for Keystone pipeline

Regulators seek to prevent potentially dangerous defects in northern leg of Canada-to-Texas project.
By JOAN LOWY, Associated Press Published: May 28, 2014
Advertisement
;

— Safety regulators have quietly placed two extra conditions on construction of TransCanada’s Keystone XL oil pipeline after learning of potentially dangerous construction defects involving the southern leg of the Canada-to-Texas project.

The defects — high rates of bad welds, dented pipe and damaged pipeline coating — have been fixed. But the federal Pipeline and Hazardous Materials Safety Administration wants to make sure similar problems don’t occur during construction of the pipeline’s controversial northern segment, which is on hold pending a decision by the Obama administration.

One condition requires TransCanada to hire a third-party contractor chosen by the pipeline safety agency to monitor the construction and make reports to the U.S. government on whether the work is sound.

The second requires TransCanada to adopt a quality management program to ensure “this pipeline is — from the beginning — built to the highest standards by both Keystone personnel and its many contractors.”

The conditions are buried near the end of the 26 appendices in a voluminous environmental impact statement on Keystone XL released by the State Department on Jan. 31.

Most of Appendix Z is devoted to 57 well-known “special conditions” that TransCanada agreed to three years ago. But conditions 58 and 59 are listed on an additional page.

The new conditions were added four months after the pipeline safety agency sent TransCanada two warning letters last year about defects and other construction problems on the Keystone Gulf Coast Pipeline, which extends from Oklahoma to the Texas Gulf Coast.

“From the start of welding, TransCanada experienced a high weld rejection rate,” said one letter dated Sept. 26. Over 72 percent of welds required repairs during one week. In another week, TransCanada stopped welding work after 205 of 425 welds required repair.

Continue reading this story on the...